Friday, September 11, 2015

Fixing My Metal Lathe

Project:
Fixing my Emco Maximat V10 metal lathe

Difficulty Level (Easy, Medium, Hard, Insane):
Easy

Process:
A few weeks ago I aquired (or should I say my wife "let" me aquire) a 1973 Emco Maximat V10 metal lathe. I knew there would be some things that required fixing and I had already fixed the Push Buttons For My Emco Maximat V10 Metal Lathe a few weeks earlier but two nights ago I was out in the shop doing some "just for the heck of it" turning (medium speed, cold rolled steel, 10 thou cut on 2 thou per revolution feed speed) and all of a sudden the lathe just stopped. It sounded like power was going to the motor (there was some humming) but the lathe had stopped turning. Of course I turned off the switch right away but I knew there was something wrong.

I started some troubleshooting and was able to turn the chuck by hand with no restriction so I knew it wasn't some locked up gear issue, and while turning the chuck by hand I could see the shaft in the motor housing turning freely so I knew the motor wasn't seized up.

After consulting with my Emco lathe peers at the Emco Lathe Yahoo Group I got a sneaking suspicion that the capacitor might be shot so I did some testing as per the video I found on youtube (link below in the Videos section) I concluded that the old capacitor was in fact deader than dead.

Fortunately, I did have a similar capacitor lying around in my spare electronics bin (I can't even remember where I got that one from, but I must have taken it off an old motor some time ago) so I put that one in and the lathe worked perfectly. The lathe started up full speed and worked as expected, except for the capacitor literally exploded about 5 minutes into my exercise with a big bang and a whole lot of smoke and everything. So I wondered if there was something wrong with the motor that causes the second capacitor to overload as well or if my "new" capacitor just didn't have the right rating. The original capacitor states "anlasskondensator" which translates into "starting capacitor" (I grew up in Switzerland so German was our official language). The only thing I could think of was that the original capacitor was rated at 330V whereas the new one was rated at only 220V. I figured that running on a 125V circuit the 220V would be sufficient, come to find out (and later confirm with my multimeter) that with A/C capacitors the voltage across the two terminals is actually about 1.6 times the rated capacity of the motor, which in my case turned out to be 267V, clearly too much for my "new" 220V capacitor.

After some more research I found out that there actually is a difference between a "Motor Running Capacitor" and a "Motor Start Capacitor" (I linked a great video from youtube that explains it well below in the Videos section). Even though the translation from german would make the "anlasskondensator" a "starting capacitor" it really should be translated as "running capacitor". Who knew?

My conclusion was that either:

1. The first "new" capacitor I used was actually a motor start capacitor instead of a motor run capacitor, or
2. The voltage rating of the first "new" capacitor was under-sized (the original was 330V and the first "new" one only 220V)

In the morning and after some calling around I actually found a local store (Wolsley) that sells parts for HVAC systems. Come to find out that these "RUNNING" capacitors are used all the time for larger motors such as A/C units and even washing machines.

I picked up the new capacitor for $27 bucks and plugged it into the lathe and there it was purring again like a 42 year old kitten. The chips were flying and the old capacitor (manufactured in October 1969) is now laying on my work bench awaiting to be taken apart with my son some other day.

Videos:




Pictures:
The two capacitors in the back of the lathe above the motor (the smaller one is for the milling attachment)
Closeup of the lathe capacitor stating 10/69 as the manufacturing date (!)
No resistance across the terminals indicates dead capacitor
Size comparison with the new capacitor (brown) that I had lying around in my electronics bin
Testing the new capacitor
The new capacitor all tucked away
5 minutes later the smoke was rising from the exploded "not-so-new-anymore" capacitor

After I opened the rear, the smoke was pretty intense
Both (now) blown capacitors
The writing on the two original capacitors. The 20uF capacitor is for the milling attachment
The new properly sized motor running capacitor
Tools:
Screw driver
Knife
Wire stripper
Wire crimper

Materials:
Two 6" pieces of wire
3 wire clamps
1 new capacitor

Cost:
$26.79

Time:
2hrs

Savings:
At least $100 bucks over if I had to call an HVAC guy to come replace the capacitor

Conclusion:
Success. I hope it will last a little longer than the last "new" capacitor

Wednesday, September 9, 2015

Scrap Metal Storage Shelf

Project:
Building a shelf for all my scrap metal pieces

Difficulty Level (Easy, Medium, Hard, Insane):
Easy

Process:
About 5 years ago I bought some 6" sonotubes, cut them to 2ft lengths and tied them together with some ratchet straps to store my scrap metal. However, over the years, the weight of the metal squished the cardboard sonotubes and the shelf started leaning forward. It was getting worse and worse to the point where you would just lightly bump the shelf and the scrap metal would slide out so I knew I'd need to re-visit my scrap metal storage solution.

I liked the concept of using sonotubes because they're fairly cheap but they're not strong enough to hold the weight of all the scrap metal so I figured I could weld a solid shelf out of 3/4" by 3/4" square metal tubes for the strength but then use sonotubes cut in half I could create 35 compartments into which I could organized all the different types of scrap metal to find it easier.

I cut up eighteen 30" pieces, welded them horizontally every 4" to create 7 shelves, cut the sonotubes in half and then to 2ft lengths. All I had to do is slide them into the shelf and put in the metal.

Pictures:
The sides of the shelf
The front of the welded shelf
The new 12' sonotubes to replace the rest
The old, sad looking scrap metal storage
Another view of how it's leaning forward and squished
The old sonotubes that are all squished up
The welded shelf before putting in the sonotubes
After the first row of sonotubes was placed in the shelf
After all the sonotubes were placed in the shelf
The finished shelf in its place
After the scrap metal was sorted, organized and placed in the shelf
A close-up of the sorted scrap metal. From the bottom up:
Solid square, solid round, flat, angle, hollow square, hollow round
Tools:
Table saw
Angle grinder
Belt sander
MIG welder
Clamps
Soap stone pencil
Square
Measuring tape

Materials:
45' of 3/4" x 3/4" square tube (cut into 18-30" pieces)
7' of 1"x1/8" angle iron (cut into 4-20" pieces)
3-6" sonotubes, 12ft long (cut in half and then into 36-2ft pieces)

Cost:
$75.00 ($27 for square tube, $4 for angle iron, $36 for sonotubes)

Time:
3hrs

Savings:
Not sure what this would have cost

Conclusion:
Love it; now I can finally find my stuff!

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