Tuesday, September 13, 2016
DIY Sheet Metal Brake
Difficulty Level (Easy, Medium, Hard, Insane):
Easy
Process:
While I was Converting my Manual Gare Kiln to PID Controller Programmable Kiln i had need of a sheet metal brake. I considered the option of bringing it to a shop and pay them $20 bucks to bend a piece of metal for me but since I've always wanted a sheet metal brake I decided to put in a few hours of my time and $20 bucks in metal to make my own.
There are some ridiculously huge, strong, heavy and expensive metal brakes out there but since I'll probably only need to use it once or a twice a year I decided to build a smaller one that screws right into my welding bench, similarly to my Benchtop Buffer/Polisher that I had built a few years back.
The process was pretty simple. I took a 2.500" wide and 3/8" thick piece of flat steel, cut it on my Metal Band Saw to 36" wide and cut a 45 degree angle on one side. At first I put a cut-off wheel in my table saw and set it at a 45 degree angle but my saw wasn't powerful enough and I didn't want to take any chances of burning out the motor (not like I've done that TWICE before)!
Once I realized the table saw wasn't gonna cut it I took the long road and did it all by hand. first with a 1/16" of an inch thin cut-off blade, then with a more solid grinding wheel (still on the angle grinder). That took me about an hour or so.
Afterwards, I drilled two holes through the metal piece as well as the welding table and tapped the holes in the welding table for a 1/2" by 13 TPI bolt.
Next, I welded a 3ft. long piece of 1.500" by 1/4" angle iron on top of it to strengthen it. Then, I used my fixed Emco Maximat V10 Metal Lathe with its Milling Attachment to make 4 pivot pieces. Each is 2" long by 5/8" thick.
After welding those 4 pieces to another, 4" longer, piece of 2.500" by 3/8" flat steel with my MIG welder and MIG Welder Cart I made 2 bushings that would fit the protruding pivot points.
All I had to do now was tack-weld the bending piece to the welding table, then slip the bushings over the protruding pivot points, and weld the bushings to a piece of 1/2" by 1" wide and about 4" long flat bar on each side.
I skipped welding handles on the brake and instead used a large adjustable wrench. Again, I'm not planning on using it a lot, but it served its purpose in making a new case for the kiln and it packs up nice and tight into a small bundle for easy storage.
Pictures:
Tools:
Angle grinder
Metal band saw
Lathe & accessories
Drill press
Drill
Measuring tape
Markers
Square
Digital calipers
MIG welder
Eye & ear protection
Bench top vise
Socket set
C-clamps
Materials:
7 feet of 2.500" by 3/8" flat iron - $15.00
4 feet of 1.500" angle iron - scrap pile
4 feet of 1.500" square tubing - scrap pile
1 foot of 1" diameter round stock - scrap pile
1 foot of 1" by 1/2" flat bar - scrap pile
Cost:
$15.00
Time:
4 hrs
Savings:
$300
Conclusion:
It works really well and I'm glad to have one more tool in my repertoire of tools
Easy
Process:
While I was Converting my Manual Gare Kiln to PID Controller Programmable Kiln i had need of a sheet metal brake. I considered the option of bringing it to a shop and pay them $20 bucks to bend a piece of metal for me but since I've always wanted a sheet metal brake I decided to put in a few hours of my time and $20 bucks in metal to make my own.
There are some ridiculously huge, strong, heavy and expensive metal brakes out there but since I'll probably only need to use it once or a twice a year I decided to build a smaller one that screws right into my welding bench, similarly to my Benchtop Buffer/Polisher that I had built a few years back.
The process was pretty simple. I took a 2.500" wide and 3/8" thick piece of flat steel, cut it on my Metal Band Saw to 36" wide and cut a 45 degree angle on one side. At first I put a cut-off wheel in my table saw and set it at a 45 degree angle but my saw wasn't powerful enough and I didn't want to take any chances of burning out the motor (not like I've done that TWICE before)!
Once I realized the table saw wasn't gonna cut it I took the long road and did it all by hand. first with a 1/16" of an inch thin cut-off blade, then with a more solid grinding wheel (still on the angle grinder). That took me about an hour or so.
Afterwards, I drilled two holes through the metal piece as well as the welding table and tapped the holes in the welding table for a 1/2" by 13 TPI bolt.
Next, I welded a 3ft. long piece of 1.500" by 1/4" angle iron on top of it to strengthen it. Then, I used my fixed Emco Maximat V10 Metal Lathe with its Milling Attachment to make 4 pivot pieces. Each is 2" long by 5/8" thick.
After welding those 4 pieces to another, 4" longer, piece of 2.500" by 3/8" flat steel with my MIG welder and MIG Welder Cart I made 2 bushings that would fit the protruding pivot points.
All I had to do now was tack-weld the bending piece to the welding table, then slip the bushings over the protruding pivot points, and weld the bushings to a piece of 1/2" by 1" wide and about 4" long flat bar on each side.
I skipped welding handles on the brake and instead used a large adjustable wrench. Again, I'm not planning on using it a lot, but it served its purpose in making a new case for the kiln and it packs up nice and tight into a small bundle for easy storage.
Pictures:
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Cutting the 2.500" by 3/8" flat bar |
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Setting the table saw at 45 degrees with a metal cut off blade didn't end up working out |
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The metal cut and ground to 45 degrees |
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A close-up view |
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Tapping a 1/2" by 13 TPI thread into the welding table |
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Fitting the angle iron on top of the flat bar |
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The pivot points after they were turned and milled to size |
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Another view |
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Close-up of the pivot points |
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After the angle iron was welded to the flat bar |
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Tack welding the pivot points to the flat bar that does the bending |
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Turning and drilling the bushings for the pivot points |
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The bushing slipped onto the pivot point |
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In position, ready to weld to the smaller flat bars of steel |
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Another view |
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Another view |
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Welding the bushings to the pieces of flat bar that would screw into the table to hold the bushings in place |
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Doing some test bends with 20 gauge sheet metal, about 16" wide |
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Another view |
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Getting ready to bend the pice of sheet metal for the kiln |
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Another view |
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The final shape |
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View from the back |
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Another view |
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Bending the air vents at the top and bottom of the piece I had just bent for the kiln |
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The front view |
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Another view |
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The vents installed |
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Close-up of the vents |
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The packed up metal brake ready to hit the storage shelf |
Angle grinder
Metal band saw
Lathe & accessories
Drill press
Drill
Measuring tape
Markers
Square
Digital calipers
MIG welder
Eye & ear protection
Bench top vise
Socket set
C-clamps
Materials:
7 feet of 2.500" by 3/8" flat iron - $15.00
4 feet of 1.500" angle iron - scrap pile
4 feet of 1.500" square tubing - scrap pile
1 foot of 1" diameter round stock - scrap pile
1 foot of 1" by 1/2" flat bar - scrap pile
Cost:
$15.00
Time:
4 hrs
Savings:
$300
Conclusion:
It works really well and I'm glad to have one more tool in my repertoire of tools
Monday, August 29, 2016
Fixing Worn Out Cross Slide Screw for a 1906 Rahn Mayer Carpenter Lathe
Difficulty Level (Easy, Medium, Hard, Insane):
Medium
Process:
A gentlemen in town contacted me about this old 1906 Rahn Mayer Carpenter metal lathe he had with a worn out cross slide screw so I had a look at it and even though the female part was bronze, both, the female bronze as well as the iron male part of the screw were completely worn out to the order of almost 0.100" slop.
Needless to say, he experienced some chatter when using the lathe. The cross slide screw looked like it was a left-hand, 3/4" diameter, 8TPI screw with a square thread. I told him that unfortunately I wasn't equipped to cut that type of thread, but what I ended up doing was to cut off the existing thread, turn it down to 9/16" and cut a regular 60 degree, 8TPI thread into the rod. Then, I cut off a 3" piece of 1" brass, turned it to down to 7/8" diameter, drilled a 7/16" hole and used a custom tap I had made out of O1 tool steel just for this purpose.
Then, I drilled and bored the worn out female thread of the brass piece and press-fit the new bushing (with the internal 9/16" by 8TPI thread) into the existing bronze part. All that was left was to cross-drill a 3/16" hole through both, the original bronze part and press in a roll pin to lock the new brass bushing to the bronze part.
Originally, I was going to use regular mild steel for the bushing but because I made the tap out of O1 tool steel, and because the 8TPI threads were quite coarse, I opted for using brass instead. In retrospect, I'm glad I did because I don't think my tap would have been strong enough to cut through mild steel.
Videos:
Pictures:
Tools:
Metal lathe and accessories
Metal band saw
Propane burner
Dividing head
Adjustable wrench
Oxy/Acetylene torch
Parts washer
Alan keys
Wire brush
Hammer
Belt sander
Hand file
Drill bits
Angle grinder
Eye & ear protection
Bench vise
Materials:
3" of 3/4" O1 tool steel
3" of 1" brass
3/16" roll pin
2L of old motor oil
Cost:
$10.00
Time:
12 hrs
Conclusion:
It looks really nice and there's zero slop in that screw now. I'm sure he'll be happy to be able to use his old lathe again
Medium
Process:
A gentlemen in town contacted me about this old 1906 Rahn Mayer Carpenter metal lathe he had with a worn out cross slide screw so I had a look at it and even though the female part was bronze, both, the female bronze as well as the iron male part of the screw were completely worn out to the order of almost 0.100" slop.
Needless to say, he experienced some chatter when using the lathe. The cross slide screw looked like it was a left-hand, 3/4" diameter, 8TPI screw with a square thread. I told him that unfortunately I wasn't equipped to cut that type of thread, but what I ended up doing was to cut off the existing thread, turn it down to 9/16" and cut a regular 60 degree, 8TPI thread into the rod. Then, I cut off a 3" piece of 1" brass, turned it to down to 7/8" diameter, drilled a 7/16" hole and used a custom tap I had made out of O1 tool steel just for this purpose.
Then, I drilled and bored the worn out female thread of the brass piece and press-fit the new bushing (with the internal 9/16" by 8TPI thread) into the existing bronze part. All that was left was to cross-drill a 3/16" hole through both, the original bronze part and press in a roll pin to lock the new brass bushing to the bronze part.
Originally, I was going to use regular mild steel for the bushing but because I made the tap out of O1 tool steel, and because the 8TPI threads were quite coarse, I opted for using brass instead. In retrospect, I'm glad I did because I don't think my tap would have been strong enough to cut through mild steel.
Videos:
Pictures:
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Close-up of the name tag and gear ratios |
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The cross slide taken apart |
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The cross slide knob |
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The old screw and block |
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Another view |
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Close-up of the banged up woodruff key |
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After the cross slide screw and handle were taken apart |
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Removing the existing worn thread |
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The old thread almost gone |
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Another view |
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Starting to cut the new thread |
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The finished screw |
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Close-up of the new thread |
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Another view of the cross slide screw |
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Another view |
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Close-up of the worn gear in the bronze block |
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Getting ready to cut the thread in the custom tap |
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Another view |
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Milling the relief cuts into the tap |
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Close-up of the relief cuts |
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Cleaning up the threads after the relief cuts were made |
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Another view |
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Done and ready for heat treating |
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Heating the tap in the propane burner |
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The hardened tap, ready for tempering to light straw color |
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The finished tap |
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View from the bottom |
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Side view of the finished tap |
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Cutting 3" of 1" brass stock |
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Facing the end and center drilling it |
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Turning the stock to size |
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The brass piece turned to 0.870" and drilled to 7/16" |
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Getting ready to tap the left handed 9/16" by 8 TPI thread |
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About half-way done |
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The finished bushing |
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That on the left will have to go into that on the right |
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Boring the hole to 0.868" |
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The finished brass piece ready to be pressed into the bronze block |
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Aligning the drill to hit half of the bronze block and half of the brass bushing |
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You can see the difference between the bronze and the brass |
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After a 3/16" roll pin was inserted to lock the brass bushing into the bronze block |
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The finished piece |
Tools:
Metal lathe and accessories
Metal band saw
Propane burner
Dividing head
Adjustable wrench
Oxy/Acetylene torch
Parts washer
Alan keys
Wire brush
Hammer
Belt sander
Hand file
Drill bits
Angle grinder
Eye & ear protection
Bench vise
Materials:
3" of 3/4" O1 tool steel
3" of 1" brass
3/16" roll pin
2L of old motor oil
Cost:
$10.00
Time:
12 hrs
Conclusion:
It looks really nice and there's zero slop in that screw now. I'm sure he'll be happy to be able to use his old lathe again
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