Wednesday, June 3, 2015

Fixing Leak On My Delonghi EAM4500 Cappuccino Machine

Project:
Replacing the leaking silicone gaskets on my cappuccino maker

Difficulty Level (Easy, Medium, Hard, Insane):
Easy

Process:
It's been about three years since I've last had to fix a Cappuccino Maker Leak so I didn't mind hauling out the tools for a good maintenance job. This time it certainly went quicker because I knew exactly what to do.

I spent a LOT of time researching and thinking about what kind of material I could use for a gasket last time around so this time it was just a matter of taking it apart, cutting the new gasket and putting it back together.

Pictures:
The parts that were taken off the machine
The machine without its covers
The old heating element gasket
The place where the heating element normally sits
Sand paper on my surface plate
Cleaning up the heating element
After the 2 heating element halves were refinished
The silicone baking pan I used for the special heating element gasket
Cutting it to approximate size
Applying the engineer's blue to the heating element
The imprint of the heating element clearly showing where the gasket goes
The old and the new gasket side by side
The new gasket installed in the heating element

Brewing a beautiful cup of java

Tools:
Screwdriver
Needle nose pliers
Socket set
Swiss army knife
Granite surface plate
Smooth small paint roller
Scissors
Utility knife
Tap & die set

Materials:
9" silicone baking pan for gasket material
O-rings
KY (water-based, food grade, to lubricate o-rings)
Engineer's blue (paint)

Cost:
$9.99

Time:
2.5 hrs

Savings:
$350.00

Conclusion:
Hope it lasts for another 3 years...

Tuesday, May 19, 2015

Fixing My Sewing Machine

Project:
Fixing the bobbin pin drive mechanism of my (yes, my, not my wife's) brother sewing machine

Difficulty Level (Easy, Medium, Hard, Insane):
Medium

Process:
The final stage of my Backyard Sun Shade Pergola project required me to sew the shade cloth to size which wouldn't have been a problem except for somehow my sewing machine stopped working. For those that don't know how to use a sewing machine, there are two places where the thread goes:

1. At the top on the actual spool
2. At the bottom in the bobbin

So when I wanted to transfer some of the uv-resistant thread to the bobbin, I put it on the bobbin pin, engaged the machine and although I could hear the machine spinning, the actual bobbin didn't spin.

After some investigation I found that somehow (and this is really weird), the rubber wheel that made a connection with the drive gear seemed to have melted off. I know it didn't actually melt because the machine never got hot enough. It almost looked like the rubber of the wheel was dissolved and dripped down into the machine. It was very sticky and gooey, kind of like asphalt. Because of that, it wasn't making proper contact with the drive wheel anymore and prevented me from filling up the bobbin with the thread I needed to sew the shade cloth.

The trickiest part was to find all the screws that held the two halves of the machine together, take those apart and then remove the drive wheel.

Once I had the bobbin pin out, I found a rubber seal/gasket that fit from one of my multi-purpose gasket kits, slipped it onto the bobbin pin and put it all back together.

Pictures:
After the two halves were separated
The bobbin pin from the top
The rubber wheel that somehow dissolved or melted
A close-up of the bobbin pin rubber wheel
Once the bobbin pin was removed
The rubber washer I put on the bobbin pin
A close-up of the new rubber "wheel"
Once the bobbin pin was installed again
Sewing the shade cloth for my backyard sun shade (link at top)
Close-up of the sun shade being sewn

Tools:
Philips screwdriver
Flat-head screwdriver
Needle nose pliers

Materials:
1 rubber gasket

Cost:
$0.02

Time:
1.5 hrs

Savings:
Not sure, but probably at least $100 bucks

Conclusion:
Works like a charm and the shade cloth is now all done

Backyard Sun Shade Pergola

Project:
Building a sun shade pergola in our back yard for my wife

Difficulty Level (Easy, Medium, Hard, Insane):
Medium

Process:
My wife has always wanted some sort of a sun shade area in our back yard so she can watch the kids play and since our girl is still a bit too little to stay on our property without constant supervision, watching her from the deck just wasn't so practical.

I had been planning this for quite some time now, composed a sketch, got Mel's stamp of approval and then put together the lumber order.

This long weekend was a long-awaited (and I must say well-deserved) get-away trip for my wife and her sister. They were gone from Thursday afternoon until Monday evening all by themselves, no kids and I thought this would be the best time to surprise her with a fully finished shade area now that the weather is finally getting a bit nicer.

After they left I called the home depot to deliver my lumber just to find out that they couldn't do it until after the weekend so I had to improvise by packing up the 3 kiddos and lugging the lumber home in a few trips in the back of the van. NOT exactly what I had envisioned but once I got a project in the "GO" stage there's no stopping.

Thursday: After the first load of lumber was at my house and the girls were in bed I built a rigid frame and got my son to help me use a laser level (once it got a bit darker) to mark the 4 corners of the pergola perfectly level.

I dug out some 16"x12" pits, 8" deep and filled them up with 4" of gravel topped by 4" of concrete to the perfect height the back posts needed to be. Then I dug 4 holes (by hand, with the help of my neighbor's manual post hole digger and the kids who loved playing in the dirt), two feet deep and filled them with 4" of gravel and a 4" concrete base.

Friday: The next day, After another trip to the home depot with all the kids, I had the materials to get the basic frame started. I put up the posts and the support beams that would hold the rafters onto the concrete pads that had hardened enough to support their weight.

Once that was all done, I bundled up the girls (Nate stayed with a friend at his house), and drove up to Goguen Lumber in Cocagne to pick up the lumber for the roof as well as the railing because it literally saved me about $400 bucks than buying the lumber from the home depot. I should mention though that the price comparison is not quite "fair" as the home depot lumber would have been pressure treated whereas the lumber from Cocagne was not.

Once I had all the lumber at home and all the kids fed, bathed and put to bed I continued building the roof, then packed up for the night around 9:30

Saturday: After breakfast, while the girls were sleeping I spent about an hour in the shop cutting up the 4x2's into 2x2's and dato'ed the bottom and top plates for the railing. Once that was all done and the kids were fed I took them outside with me. While they played Nate and I finished the top of the roof and prepared the railing.

Once the girls were in bed (around 6:30) I put together the railing, the support struts for the roof, cleaned everything up and called it a night, again, around 9:30.

Monday: After a wonderful day off on Sunday and a great breakfast on Monday morning I filled in the area around the posts and cut up the shade cloth that I had ordered a few years ago for another one of my projects. Once I had it all cut to proper size, I wanted to sew up the edges nice and clean just to find out that something was wrong with my sewing machine so I had to Fix My Sewing Machine first. After that was done, all I had to do was put some hooks in the corners of the pergola and hang up the shade cloth. I am very pleased with how it turned out and my wife was very surprised and very happy with it.

Videos:

Pictures:
A sketch of what I envisioned
After I dug out the 3 patches for the rear posts
After the 8" holes were filled with 4" of gravel
Getting the kids to dig in the dirt for the front holes (they loved it)
First trip to home depot with the kids
After the vertical braces were installed for levelling
Installing the front 4x4 posts
The van loaded with lumber
After the roof rafters were installed
Getting ready for the 2x2s at the top
The kids observing
Half-way done with the 2x2s
After the 2x2s were installed
A view from the deck
Getting ready to install the railing
After the railing was almost done
All done
A view from the top bedroom
Close-up of sewing the shade cloth
After the shade cloth was hung up
Another view from the inside of the pergola

Tools:
Pick ax
Shovel
Bucket
Wheel barrow
Angle grinder with diamond blade
Drill
Hammer
Chop saw
Manual post hole digger
Van
Table saw with regular and dato blade
Chalk line
Level
Air nailer
Framing nailer
Compressor
Extension chords
2' step ladder
6' step ladder
16' extension ladder
Measuring tape
Pencil

Materials:
3 - 4x4-8' pressure treated (pt)
4 - 4x4-10 pt
2 - 2x8-24' pt2 bags of portland cement
2 wheel barrows of gravel
1 wheel barrow of sand
13 - 2x6-12'
20 - 2x4-8'
35 - 1x6 fence boards
10 - 2x4-10' pt
4 - 2x4-8' pt
2 - 4x8 sheets of "privacy plus" lattice
Galvanized 3-1/4" nails
3" Screws
6 - 6" lag bolts with washers
6 hooks
10'x14' shade cloth (80%)
1-1/4" staples for privacy lattice

Cost:
$600.00

Time:
25 hrs

Savings:
Probably at least $1000 to $1500

Conclusion:
It's really idyllic

Monday, April 27, 2015

Saving the Microwave at Work

Project:
Fixing the start button on the microwave from the kitchen at work

Difficulty Level (Easy, Medium, Hard, Insane):
Easy

Process:
For about two and a half years the one microwave at work has been giving everyone a hard time in starting. After some time we all found the way to push the button just right (on the left push towards the center and down a bit) to get it working, sometimes after up to 15 seconds of fiddling around.

Well, I was off on leave for the last 9 months and kinda gotten used to getting stuff done so when I came back and saw that the microwave was still being a pain in the butt (well, a pain in the "finger" would be more accurate because you had to push that silly button so bloody hard...), I decided to have a "look" at it once and for all.

Out came the Swiss army knife during my lunch break and I took that thing apart just to find out that the soldering connection of one of the little metal connectors had broken loose. So I took the electronic display module off and took it home with me over the weekend, soldered it back in place and put it all back together Monday morning.

The lunch room conversation has been quite the entertaining event to say the least. I'm very pleased, not only that we saved the citizens of canada about $130 bucks but that we can now get through the lunch wait line twice as fast! Yeah for Swiss army knives and soldering irons!

Pictures:

The broken microwave in all its glory
After I took the case off
After I took the keypad module out
The keypad module
The broken connection (red circle)
Another view of the broken solder connection (red circle)
After it was soldered back on
Back in the kitchen fully functional

A nice coworker even made me a sign


Tools:
Swiss army knife
Soldering iron

Materials:
1/4" of soldering rod

Cost:
$0.00

Time:
20 minutes

Savings:
$130.00

Conclusion:
It better last or they'll be laughing at me during lunch time...

Sunday, April 19, 2015

Bedroom Window

Project:
Fix our bedroom window

Difficulty Level (Easy, Medium, Hard, Insane):
Easy

Process:
After one of our ridiculous snow storms back in February I was out on the back snow blowing my deck and noticed that somehow the bedroom window was cracked. We put a piece of black plastic on the inside to block out the light which (I'm assuming) heated up the window to such a high temperature that it cracked. That would also be the reason I didn't notice it until looking at it from the outside.

On one of my trips to Home Depot with my two oldest kids I asked the window guy if there was a way to just replace the window pane and not having to take the entire window out of the house so he showed me and it was actually remarkably easy to do.

Ordering the window took a little while, but the guys at Mitten (formerly Procana) have always been excellent in helping me out. And, they charged me less than $50 bucks. Way less than any other window place (the highest quote I got for the same window was $180 + tax)

All I had to do is jam my Swiss army knife can opener between the frame and the trim of the window, remove the 4 plastic trims, pull out the old pane, put the new one in and re-install the trim.

Aside from the double-sided tape that made it a little bit tricky to get the old window out and a few minutes of cleaning up that tape it went pretty smooth and was done in under an hour and less than $50 bucks.

Pictures:
The broken window pane
The plastic trim holding in the pane with some black duct tape residue
After the trim was removed 
After the window frame was cleaned up
Putting new double-sided tape on the frame
A view from the bedroom
The new window pane
After it was installed and putting the blackout plastic pieces back on

Tools:
Swiss army knife
Screwdriver
Hammer

Materials:
New window pane
Double sided foam tape

Cost:
$47.53

Time:
1hr

Savings:
Probably at least $100 bucks

Conclusion:
New and shiny now!

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